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Innovation Saves the Day!

The task of the CCS crew was to remove a failed liner using a robot water blaster.  When the robot became lodged in the failed liner, it was time to call in professional divers to dislodge the robot - and remove the liner. The pipe was 21" RCP at a depth of 12' and 16' up the line. 

As always, safety was our number one concern.

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